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Reply to "Great Northern railway"

PM another engine.

GN N-3 2-8-8-0 made by Tenshodo in 1973.  TCS 1517 decoder, re-gear, re-motor, lots of LED lights and Glacier paint added.

This engine was, occasionally, shorting at the last 'OPS'.

Videos:

Skykomish:

https://www.youtube.com/watch?v=_qHm2YUmYTw

Hillyard:

https://www.youtube.com/watch?v=k7liWQpnGjk

While in a tunnel, I noticed the 'blow down' pipe was below rail 'level'.  That was adjusted but nada.

GN N-3 2-8-8-0 Tenshodo 58

'Blow down' pipe.

GN N-3 2-8-8-0 Tenshodo 59

While on a trestle, I started wiggling the engine with no results and then the tender and noticed a tiny spark where the draw bar screw nut was, momentarily, making contact with the engine frame, thus causing the short.  The draw bar screw just had to be tightened while securing the nut and all's 'good'.

GN N-3 2-8-8-0 Tenshodo 60

The Seattle's freight yard was full so the 'freight drag' was routed to St. Paul's freight yard.

GN N-3 2-8-8-0 Tenshodo 61

Attachments

Images (4)
  • GN N-3 2-8-8-0 Tenshodo 58
  • GN N-3 2-8-8-0 Tenshodo 59
  • GN N-3 2-8-8-0 Tenshodo 60
  • GN N-3 2-8-8-0 Tenshodo 61
Last edited by samparfitt
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