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I was thinking about putting a YLB into the tender of my new H10, so I flopped it on to my work cradle. 

OOPS, it seems that the power screwdriver got away from someone at the factory!  I'll have to dig out my removal bit to get this one out if I want to get into the tender!

 

The other screws all seem fine, so apparently he figured out the torque setting after the first screw.  

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Yikes!  Just yesterday, I was looking at the Western Allegheny H10 in the showcase of Express Hobbies in Cranberry Township, Pa.  Very nice looking, and a regional favorite for Butler County, but I'm not in the market for one myself.  I'll keep an eye out to see what screw remover you use also.  Reminds me of I guy I worked with in the '70s.  He was called "Torque" O'Donnell for obvious reasons.  Nice guy, though.  They made him a manager long ago....

Last edited by Mark Boyce

Actually John, this "worker' was just following the specification of "one quarter turn past shear" during assembly.

I ran into this same issue trying to remove my SP SD45 shell recently to repack my smoke unit. The screws are ultra small ( like 2mm heads) and also made out of "soft aluminum" material ( or so it seemed). The only way I got them out was to take a Dremel rotary disc and cut straight slots into the heads which allowed enough torque to get them removed. Fortunately, this was just before the November parts sale, so I ordered a few dozen for the next time I have a screw-removal adventure.....

For those who have asked about removing the screw. I have had a lot of success over the years with this unit from Black and Decker: (I bought it from Sears 7-8 years ago)

Unfortunately it has since been Discontinued but it has been a life saver for me over the years I have owned it. I purchased it to remove the steering column from a 1977 VW Bay Window Bus I had and since then have used it countless times.

It involves drilling a small hole (Depending on the remover you will use) in the head of the stripped screw, which is the hardest and most critical step. Once you have a deep enough hole, these reverse thread extractors will dig deeper into the hole you drilled while at the same time turning the screw counter clockwise, aka removing it.

Hope this helps!

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Daniel J. Gonzalez posted:

For those who have asked about removing the screw. I have had a lot of success over the years with this unit from Black and Decker: (I bought it from Sears 7-8 years ago)

Unfortunately it has since been Discontinued but it has been a life saver for me over the years I have owned it. I purchased it to remove the steering column from a 1977 VW Bay Window Bus I had and since then have used it countless times.

It involves drilling a small hole (Depending on the remover you will use) in the head of the stripped screw, which is the hardest and most critical step. Once you have a deep enough hole, these reverse thread extractors will dig deeper into the hole you drilled while at the same time turning the screw counter clockwise, aka removing it.

Hope this helps!

Daniel back in the day they were called "easy out's" Still available on Amazon. Nick

Last edited by rockstars1989

Goodness, it gets worse!  After I removed the two mangled screws, I popped the top and... SAY WHAT???

On the bottom, you can see what is pressing on that wire.  FYI, that gray wire is the track center roller!  Imagine if those two got together! 

Goodness, I patched the wire and figured I dodged a bullet.  I also took 1/8" off the mounting sled for the RailSounds board so there's a bit more clearance for the upper and lower connectors.  I think the Mechanical engineers at Lionel need to go back for a refresher course on clearances!

I thought I was all done, but I noticed a flash of something metallic looking by the coupler.  Better check that out...

OOPS!  A little more ham-handed assembly it would appear.  I think you can only pull on those wires so much before they pull out of the coupler!  Time to dive into the parts box again.

Good grief!

I can hardly wait to see what the inside of the locomotive looks like!  The tender should have been a piece of cake to allow proper clearances!

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I suspect about the 3rd time I fired the coupler, it would have been the last time!  As for the other wire, I was pretty blown away that they forced these together like that.  The amazing part is every one is probably jammed together like this, I can't imagine what would be different, both sides are securely mounted in that precise orientation!

Yes, I'm also replacing the two screws that are buggered up, one wasn't as bad, but I got them both out.  A brand new bit has a sharper bite, managed to get the them both out.

Well.... so much for Lionel putting a QA team in place.

Not much in the way of operational complaints(yet).  These things are looking like the FP 40s all over again. A disaster waiting to happen.

I'm waiting to see what you find under the boiler.

Mine is still sealed in the shipper . I'm about 2 more "H10 issue"posts away from selling it.

What a disappointment.

Last edited by RickO
RickO posted:

Well.... so much for Lionel putting a QA team in place.

Not much in the way of operational complaints(yet).  These things are looking like the FP 40s all over again. A disaster waiting to happen.

I'm waiting to see what you find under the boiler.

Mine is still sealed in the shipper . I'm about 2 more "H10 issue"posts away from selling it.

What a disappointment.

I feel you my friend. The other posts didn't concern me too much and the stripped screw didn't turn me off too much either but the bad wiring does. It's like Lionel wants them to work and eventually fail, hopefully after the warranty period.

I know that's not the case but it just looks a such IMO.

Hope mine doesn't look like yours John. What a mess.

What I can only hope it the final chapter.   Well, at least for the tender, who knows what the inside of the locomotive looks like!

I went to put it back together after replacing the coupler, fixing the wire, and cleaning up the other wire.  Even with taking some meat off the bottom of the RS board holder to lower it's profile, something was still hitting, and the tender frame was rocking and I couldn't seat it.  After a few more measurements, it became clear, it's the big capacitor on the RS board, it was running into the PCB for the volume control and lighting.  Short of losing the holder totally, there will never be enough clearance.  Since the screw that holds the tender on is under there, and it needs clearance, I went with a compromise.  I canted the board to one side so the connectors didn't clash, and angled it so the capacitor missed the upper PCB.  Now the tender shell goes on without hitting anything.

One wonders how they got any of these together without wrecking something with those clearance issues!

Since I was already in there, I treated my self to a shorter coupler, looks better coupled up to rolling stock.  I suspect it might no do tight curves, but I'm not planning those anyway.

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Last edited by gunrunnerjohn

Well, some of it is an individual thing, but the clearance issues doubtless affect all the units, so that's going to come along and bite them in the butt before long!  Sadly, it's probably going to bite the owners in the butt harder than Lionel as it's likely some of these failures won't manifest themselves before the warranty runs out.   All of this would have been avoided if they mounted the RS board at a 90 degree twist, it would fit inside the shell that way.  That would have taken care of all the clearance issues.  They would have needed a different plastic mount with the mount on the side, but I suspect that would be cheaper than fixing all of these.

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