So I hope I'm doing the correct thing by adding to this post and if not I do apologize.
About a year ago I was in the midst of really getting into the o gauge scene. As with most of us, my first set was a PE starter set. Well the fever quickly grew and I started my hunt for a diesel loco, more track, etc.
Well my uneducated search lead me to a Lionel Factory Refurbished UP GP38 w/LC+ (INSERT POOP EMOJI) and at first all was ok, the unit came damaged (I am the reason Lionel added a discalmer that the Refurbished locos were 100% mechanically but not physically, the never said that last part until I complained about it to them). After a bit of use the engine started to give me intermointer issues like no smoke or rapid takeoff, so I decided I was done with LC+ and that I was going to go command from now on. Well I purchased a PS2 Diesel and fell in love with it and MTH. Next step was to purchase DCS, check. Next I decided to sink my teeth I to a PS3 Upgrade kit for the POS LC engine.
Let me start off by saying, it worked. I may not be a MTH Certified Rapair Guy or Gal but I do know more than enough about electronics that I wasn't even nervous. Well after everything worked for a few weeks, the smoke unit stops working, pull the shell off to find my connection to be solid but where the connector hits the smoke unit, it was loose. Pushed it tight and was working perfectly. Decided to test before putting the body on and of course she ran like a top. Now here is where my story turns for the worse. I put the shell back on, put the loco on the track, apply power and...................
That is where my story ends. The unit never woke up again. No click no nothing just a faint humm and that is all. I pulled to shell to find out had pinched a motor wire and it shorted with the can of the motor.
My question is, is that it for me? Is this board Seriously done for? $200 down the toilet? Seems to me, and of course I mean this with all do respect but this could have happened to anyone including an MTH CERT TECH, NO?
I just feel as if these electronics are so sensitive, literally killed $200 because of a pinched wire that just so happened to be in a narrow part of the shell.
From what my friend GRJ and others have said, it looks like I'm up a creek without a paddle but I guess I just either needed to vent and or wanted to see what you 3 rail geniuses think are my options.
Thanks for listening and as always I hope this post helps many!
Thanks
Daniel Gonzalez