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Boy, this is really getting tiresome.  We're having a modular show this weekend, so I figured I'd run my newly "fixed" Legacy F40PH.  BUZZ, WRONG!  It's as wacky as ever!  First, when I turned on the smoke, it stopped, that's not exactly right.  However, I got it running, and then I noticed that whenever I turned off the smoke it would stop???

OK, enough of that, I'll just run it without the smoke and deal with that later.  I get all the Amtrak cars out, the F40PH, and the Cabbage unit.  I managed about a ten minute run and suddenly it stops.  Blinking out a drive motor fault!!!  OUCH!  I reset it and still no joy.  I power cycled the track, and then it was back in business, this time for about two minutes, and back to the drive motor fault!

This has been by far the most problematic locomotive I've every had, and that includes some eBay treasures where you don't know what you're getting!  Looks like yet another trip to Lionel, I wonder when the Lemon Law kicks in on these?

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John,

Try swapping out the R4LC for one you know works.  I had a TMCC F7 that after running the engine for a while, would stop and switch into Conventional Mode.  It turned out that the R2LC had a latent issue and when it got warm, it stopped working.  Swapping it out fixed it.

Just a guess...

Matt, the much better radio board that plugs into the much better RCMC board system is a great package.  Thank goodness the modular boards are fading into history.   The F-40 was made by a new company.  Any engines after that one should be improved.  I have fixed my share of those.  

Allan, that engine does not use the out dated R4LC.  That was used with old school modular boards.  It uses the RCMC board system.  That is a great system.

John, I had one where the motor would stop for no reason.  Gave it the old school try and hit the back of the motor pins on the RCMC with a hot iron and life was good.  Knowing you, I am sure you have already looked at that.  Just wanted to share.

 

 

Last edited by Marty Fitzhenry
Marty Fitzhenry posted:
John, I had one where the motor would stop for no reason.  Gave it the old school try and hit the back of the motor pins on the RCMC with a hot iron and life was good.  Knowing you, I am sure you have already looked at that.  Just wanted to share.

I haven't removed the RCMC, however I did pop the top and check all the wiring.  I was hoping against hope that something was hitting a flywheel or there was a loose plug, but all seemed well.  I tugged on all the wires to see if anything was loose in the connector, but nothing seemed amiss.

The oddity with it having drive problems when changing the smoke settings leads me to believe it's either a voltage drop or an issue on the RCMC.  This thing doesn't have an hours running time yet, I was finally going to get it out for a real run, so much for that idea!

BANDOB posted:

Guess I better take a Williams Amtrak Genesis unit as a back-up, just in case.

That's a good idea.  I have my MTH Premier Genesis that I upgraded to TMCC ready to stand in for the F40PH.  Clearly, I want to go more than 5-10 minutes at the show!

I like to get out the equipment to run at the show and make sure it's all 100% functional, glad I checked the F40PH again, it did run for 20-30 minutes a couple weeks ago, obviously it doesn't age well!

The Genesis is willing and able to pull the cars.  Probably a reason that this locomotive lasted so long in Amtrak service, it holds together better.

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Marty Fitzhenry posted:

John, I do not have that smoke unit in front of me.  Due to the fact your issue comes in with the smoke, I would look at the unit and I am sure you have done that.  If the unit has a thermister and it is hitting the element, that would be a red flag.

It's not just with smoke Marty.  I had turned the smoke off and decided to simply not use it.  After a few minutes running with no smoke, it started getting the drive motor fail code.

The issue with the smoke was the engine would simply stop at times when I changed the smoke setting.  I could get it running again by turning the throttle and I'd be moving again.

It's like it's haunted!

C&O Allie posted:

John,

Try swapping out the R4LC for one you know works.  I had a TMCC F7 that after running the engine for a while, would stop and switch into Conventional Mode.  It turned out that the R2LC had a latent issue and when it got warm, it stopped working.  Swapping it out fixed it.

Just a guess...

That is really good tip.  I have an engine that does the same thing.  It runs fine for about 20 minutes and then suddenly switches to conventional.  Of course, in command mode the voltage is turned all the way up and in conventional the engine becomes an American Flyer.

NH Joe

 

John

Im having similar issues with my CSX version. It returned from Lionel, and once again doesn't work. After you put the engine on the track, the sounds start to spaz out, and you get quite the light show. Along with that, it doesn't respond to legacy signal. Back to Lionel... I think I might just demand a new one 

J Daddy posted:

I was saved by this engines ugly looks that I never ordered one... I remember when I was a kid these came out and I thought ugh ... what a dog.

John - hope you can get yours running - good luck on the repair.

 

amtrak_f40ph_291_at_boston_south_station_by_trinityctstudios-d4ikam3

That's the only "modern" engine that I like, probably because it reminds me of a F-7 in sort of a Bizarro way.

Maxrailroad posted:

John

Im having similar issues with my CSX version. It returned from Lionel, and once again doesn't work. After you put the engine on the track, the sounds start to spaz out, and you get quite the light show. Along with that, it doesn't respond to legacy signal. Back to Lionel... I think I might just demand a new one 

Yours sounds like the wire routing issue that was chafing the flywheel.  Mine looks just fine inside, it appears to either be some flaky connector that I can't see or a problem on the RCMC.

This reminds one of prototypes where a few of the F40’s put into passenger service apparently lacked head end power for the rest of the train. Accordingly, their prime movers had to operate in run 8 at all times. Talk about a loud screamer in the station. Amtrak or Metrolink must have a survivor in standby service in SoCal because it came through Fullerton station quite recently. Everyone at the train watchers table would undoubtedly like to know what’s wrong with your model, John, so that they could recommend the flaw to the appropriate local locomotive service facility.

Sounds like its a bad receptacle in the motor harness or speed encoder harness. Id also check the solder points for the pins related to the plugs on the board. Double check that you don't have any cold solder joints I've seen that on the boards before.

If the smoke unit is acting weird it could be a bad RCMC it sounds like...unless something is grounding out.

If you get tired of dealing with them I'm willing to take a look at them

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