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Got my new UP Challenger the other day thought I’d let everyone know what I’ve found. Theses are great looking locomotives. Came unscathed from shipping.

I’m naturally curious so thought I’d open it up and poke around I tend to put some miles on my locomotives so wanted to be sure all was well.

IMG_3126

Pretty clean only two plugs to completely remove the shell.

when I pulled it out of the box I had a run away screw so I was keeping an eye out for where it belonged. Found it in a spot I didn’t expect

IMG_3129

the motor mount was missing one screw and was really loose. Got that fixed no harm no fowl yet

I assume this is the additional board for the 4 digit addressing.
IMG_3127

I then decided to take a peak in the gear box. There was basically no “grease” in there. I removed what I could and filled with some actual grease.

IMG_3130

As is from factory

IMG_3133

all the grease removed from the rear gear box

with that find I moved to the front engine. It was better but still not much

IMG_3135

this is the front engine after removing as much as possible and putting it in the top plate.

IMG_3131

to cap it off a pinched wire from the factory.

this is hear just as some information for curious minds we don’t need another bashing thread, I like this locomotive it also has two separate parts that were bagged with it that I have yet to figure out where they belong, the manual was no help unfortunately.  One looks like air hoses.

here’s a video from todays run at the club

Attachments

Images (9)
  • IMG_3126: Inside the boiler
  • IMG_3129: Missing motor mount screw
  • IMG_3128: Missing screw
  • IMG_3127: 4 digit address radio
  • IMG_3130: Factory rear gear box. There was a small. Very small blob further down past the interment gear
  • IMG_3134: Factory gear box grease
  • IMG_3135: Front engine
  • IMG_3133: All grease for rear gear box
  • IMG_3131: Pinched wire
Videos (1)
IMG_3142
Original Post

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I have to wonder about this dogbone being almost out of the joint, I'd expect some rough running.

4 digit addressing is internal to the main board, this board is the Bluetooth board, note the BT antenna.

Yes definitely a rough running with the drive like that. That was with one motor mount screw missing and the other very loose. I never ran it like that so no telling how rough it would’ve been.

John I thought the same thing that was the Bluetooth board but if you look under the wires you can see the integrated Bluetooth board with its own antenna on the LCP3 board

IMG_3145

is that new board just another Bluetooth radio strictly for stuff with the new Base 3? Maybe not necessarily 4 digit addressing, it’s just the radio board didn’t look any different than usual either so that’s what made me think that.

Attachments

Images (1)
  • IMG_3145
@zhubl posted:
is that new board just another Bluetooth radio strictly for stuff with the new Base 3? Maybe not necessarily 4 digit addressing, it’s just the radio board didn’t look any different than usual either so that’s what made me think that.

Well, their two-way communication capability is bound to require a Bluetooth back-channel, so maybe that's it.  I'm sure that the two-way communication ain't going over the track.

@zhubl posted:

As is from factory

all the grease removed from the rear gear box

with that find I moved to the front engine. It was better but still not much

IMG_3135

this is the front engine after removing as much as possible and putting it in the top plate.



Where is the front bearing?! What a joke! For a $2000 locomotive?

The chances that I preorder a PRR M1 or get an I1sa just keep dwindling…

@zhubl posted:

Yes definitely a rough running with the drive like that. That was with one motor mount screw missing and the other very loose. I never ran it like that so no telling how rough it would’ve been.

John I thought the same thing that was the Bluetooth board but if you look under the wires you can see the integrated Bluetooth board with its own antenna on the LCP3 board

IMG_3145

is that new board just another Bluetooth radio strictly for stuff with the new Base 3? Maybe not necessarily 4 digit addressing, it’s just the radio board didn’t look any different than usual either so that’s what made me think that.

Did tightening up the motor mount pull in the motor towards the gear box and take up that excessive slack in the dog bone?…..after you tightened up the motor mount, did you check to see how much end play was between the cups?….I’ve had quite a few Legacy big steam that I’ve had to build a better driveshaft ( dog bone) because even with the motor mount tight, the end play was just too excessive IMO, ….a before & after shot would’ve been handy,……

Pat

@harmonyards posted:

Did tightening up the motor mount pull in the motor towards the gear box and take up that excessive slack in the dog bone?…..after you tightened up the motor mount, did you check to see how much end play was between the cups?….I’ve had quite a few Legacy big steam that I’ve had to build a better driveshaft ( dog bone) because even with the motor mount tight, the end play was just too excessive IMO, ….a before & after shot would’ve been handy,……

Pat

My bad Pat I didn’t even think of an after picture. I was honestly shocked when John pointed out how loose it was because I specifically remember when I was done it was actually pretty tight in the cups very little horizontal movement

You know guys I don’t doubt the Pittmans being superior to the Canons but I have yet to have an issue with any of my locomotives with Canons if I do you can bet I’ll hit Pat up for a Pittman.

you know I’ve seen a Ametek building out by Sprit Aerosystems as I go between jobs. Doubt I could get any motors out of them with out selling a limb.

@zhubl posted:

You know guys I don’t doubt the Pittmans being superior to the Canons but I have yet to have an issue with any of my locomotives with Canons if I do you can bet I’ll hit Pat up for a Pittman.

you know I’ve seen a Ametek building out by Sprit Aerosystems as I go between jobs. Doubt I could get any motors out of them with out selling a limb.

You said a mouthful right there, …….the rep from Ametek actually came out & visited me, …but it took him all of 30 seconds to say thanks, but no thanks,….

Pat

That is real nice looking engine, Zachariah, and commendation to you for going through preparation and what the army calls PMCS (Preventative Maintenance checks and services).

I am curious as to what the resident forum experts think would've happened without going through PMCS on this model? To my rudimentary understanding, a pinched wire could/would result in a short, which can be serious enough to destroy circuit boards; and a loose/missing motor mount screw would result in excessive gear wear.

If it were my engine, I would let Dave Olson at Lionel know of the experience. These are premium models, and the more real-world experience of operators sharing, the better Lionel will be equipped to head these issues off.

@Paul Kallus posted:

I am curious as to what the resident forum experts think would've happened without going through PMCS on this model? To my rudimentary understanding, a pinched wire could/would result in a short, which can be serious enough to destroy circuit boards; and a loose/missing motor mount screw would result in excessive gear wear.

A pinched wire is one of the most common factory faults, and when it pierces the insulation, it will usually kill something for sure!

@zhubl posted:

You know guys I don’t doubt the Pittmans being superior to the Canons but I have yet to have an issue with any of my locomotives with Canons if I do you can bet I’ll hit Pat up for a Pittman.

I'm at 4 dead RCMC boards due to the Canon motor throwing a brush and shorting out. I did actually manage to rescue one of them by replacing the driver FETs, the other three were goners. I guesstimate out of around 60 or so Legacy steamers that's my total of 4 bad motors. That's not a batting average that I'd apply to any decent motor!

Last edited by gunrunnerjohn

I'm at 4 dead RCMC boards due to the Canon motor throwing a brush and shorting out. I did actually manage to rescue one of them by replacing the driver FETs, the other three were goners. I guesstimate out of around 60 or so Legacy steamers that's my total of bad motors. That's not a batting average that I'd apply to any decent motor!

For prospective, out of how many?  We looking at 5%, 3%, 1% failure rate?  Recent failures or when Lionel first switched?  Reason I ask you guys are gobbling up all the pittmans left in the market for something that might or might not be needed.

@superwarp1 posted:

For prospective, out of how many?  We looking at 5%, 3%, 1% failure rate?  Recent failures or when Lionel first switched?  Reason I ask you guys are gobbling up all the pittmans left in the market for something that might or might not be needed.

I'm guessing you didn't read the whole post.

I guesstimate out of around 60 or so Legacy steamers that's my total of 4 bad motors. That's not a batting average that I'd apply to any decent motor!

@superwarp1 posted:

For prospective, out of how many?  We looking at 5%, 3%, 1% failure rate?  Recent failures or when Lionel first switched?  Reason I ask you guys are gobbling up all the pittmans left in the market for something that might or might not be needed.

IMO Gary, the Cannon is straight up a gamble ……it fails in a weird way that lets the brush arm short to the can, …..that can be the kiss of death for a RCMC ….I actually had one give me a 5 minute warning by the horribly audible clicking sound like a baseball card in bicycle spokes…some of the legacy gurus say the motor driver over load  self protect kicks in, but it doesn’t do any good for dead short to ground…..load is one thing, completed path is another……😉

Pat

Well, It looks like the brush is poorly designed and can easily break off and then short things out internally.  While the RCMC has motor stall protection, Jon told me that a direct short is not able to be detected quickly enough to prevent cooking the FET motor drivers.  Obviously, Jon's the one to ask for specific details, but suffice to say that the motor short protection isn't perfect for the RCMC.  Given that fact, frequently the motor failure also takes the RCMC with it.  I believe it was Pat @harmonyards that posted a picture of the motor cracked open and how the brush breaks free and is rattling around inside the motor.

Yes, I opened mine up and discovered the fragile piece in the cheesy plastic brush holder. ….that was the end for me, ….they’ve all since been evicted. …..I have some fresh 2023 refugees here at the shop if Gary would like me to open one up,…..I doubt Cannon changed anything, and Lionel probably doesn’t care given the rate of attrition is more than likely acceptable to them nowadays ……

Pat

@harmonyards posted:

Yes, I opened mine up and discovered the fragile piece in the cheesy plastic brush holder. ….that was the end for me, ….they’ve all since been evicted. …..I have some fresh 2023 refugees here at the shop if Gary would like me to open one up,…..I doubt Cannon changed anything, and Lionel probably doesn’t care given the rate of attrition is more than likely acceptable to them nowadays ……

Pat

I’ve ask Dave at Lionel about this and if he’s to be believed Lionel is not seeing a high failure rate, are they lasting just long enough to get past the one year warranty?

@superwarp1 posted:

I’ve ask Dave at Lionel about this and if he’s to be believed Lionel is not seeing a high failure rate, are they lasting just long enough to get past the one year warranty?

All of the locomotives I replaced them in after failure were more than a year old.  Of course, many people don't run a new locomotive long enough to find out if something is going to fail in a year's time.

@superwarp1 posted:

I’ve ask Dave at Lionel about this and if he’s to be believed Lionel is not seeing a high failure rate, are they lasting just long enough to get past the one year warranty?

As John said, the ones I’ve actually seen fail are out of warranty, so I’d imagine this ain’t Dave’s problem,….Also to note, the ones I have seen fail were all folks like myself that use the models as intended…..run them!…..Some people do a parade lap one time, then back on the shelf, ……I’d venture to say most of them would last forever, maybe with the one odd failure here or there……..but anyone who’s ever visited here can attest, there’s always trains running on my layout….So eviction notices, and an ink pen are always on the ready!…..😉

Pat

@Junior posted:

HEY @gunrunnerjohn....

Is this defect visible from the outside of the motor(s)? I'd like to check out my Lionmaster Challenger that I did so much work on to resuscitate the 'ole girl'....

There is no hint of any issue from the outside until the brush falls off.  I suspect there is a very short time that the motor probably doesn't run right before the brush is completely off.  However, I've never actually been there for the failure, just cleaning up after the carnage.

@harmonyards

Hey Pat....

Yes....its designed to run on 031 curve. I'm limited to Lionmaster "Big Steam" because my layout has 054 and 072 curve mixed all through it. Sounds like I should be in the clear.

Hey.....since I have your attention....how do I go about contacting you and ask you to convert a Lionel Steamer from Pulmor to a can motor and get all the details (ie. cost)?

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