Skip to main content

I have two 1950's lower end locos (a 44 ton #628 and a SW switcher #621) that have not been run in years.  I attempted to run both last evening with limited success.  After a cleaning both respond to the transformer but run poorly at best.  The 44 ton will run in one direction well if given a gentle nudge to get it moving.  The other direction it runs slowly and loudly.  The 621 moves but under duress.  I suspect this is a gear meshing issue.  There is no issue with power pick up or with the e units.  The e units cycle normally.  I am open to suggestions and advice.  BTW, I do not remember either of these being problematic in the past.

Original Post

Replies sorted oldest to newest

You are describing a known problem with those engines. Lionel has a fix in their factory service manual. The reference is for a different loco, but the construction and problem is the same.

Here it is.

Rather than center punching, as Lionel suggests, I used to wedge paper matchsticks between the bottom plate and the motor frame to the same effect.

I am certain folks with chime in with other solutions.

Last edited by C W Burfle

Wow, thanks for the quick response.  I should have mentioned that both have been opened up and cleaned.  By cleaned I mean old grease removed and each gear individually cleaned with a fine blade screwdriver to remove the gunk.    I will have to put down a loop of 027 track and just let them circle for a bit to see of things improve.  

Have you tried to bench test these engines?

Look for excessive sparks around the brush contact area, as this can be poor contact to the armature because of not enough spring tension on the brushes. This is mainly a problem with American Flyer motors but can also happen to Lionel engines.

Stretch your springs out a little by hand, make sure both are about the same length and replace them in the motor area.

 

Lee Fritz

pappy, cleaned entire motor, top and bottom.  I use the OG mag article from years back that provides a process that is simple and methodical.  Surprisingly there was very little gunk in either motor.  There are no frayed wires or split insulation, brushes are in decent shape, the top of the motor that everyone advises to clean with some form of non abrasive has been cleaned, the motor winding is clean.  For the purpose of testing I am locking out the e unit so the motor only moves in a single direction and yes I checked to make sure it is not locked in neutral.  These motors should be bullet proof so I expect to find a solution.  Anything mechanical can be fixed with enough time and beer.

As I wrote above, the issue described by Necrails is a common and well known problem for that style motor.

Necrails can confirm it by getting the motor running in the troublesome direction, and turning it upside down. Take a finger and firmly  push the black bottom plate to one side. If the motor speeds up, you've identified the problem. If the motor still runs poorly, or gets worse, try pushing it to the other side.

 

As I also noted above, using headless paper matches to push the bottom plate in the correct direction is one way to tighten up the bottom plate. I haven't had one fall out.

The problem with center punching, as Lionel advised, is the difficulty in undoing a mistake .

 

If this test doesn't show that a loose bottom plate is the problem, then it certainly could be caused by the other things mentioned.

 

Last edited by C W Burfle

The problem is the lower bearing plate is floating in the stamped aluminum motor side frames as the factory staking has worked loose over the years.  The old Lionel fix for this was to "dent" the side frames with a punch, some shops used cardstock jammed in to firm up the plate.

 

I have had good luck using tiny black anodized self-tapping screws into drilled pilot holes to hold the bearing in place.

 

For a non-destructive fix, my latest method, though, beats them all.  Using the CRC QD or any non-residue contact cleaner, clean ALL oil & residue from between the sideframes & the bearing, using the nozzle to spray into the crevice.  Dry it out well, several hours or overnight.

 

Now use the regular "thin"(not gel) CA adhesive("Super Glue", Eastman 910, etc.) and flow the cement into the crevice on both sides, letting it creep in by capillary action to fill the gap.

 

In about 10 minutes, the loco is ready to be lubed(grease on gears, oil on pivots & bearings/axles) and will run like new. 

Add Reply

Post

OGR Publishing, Inc., 1310 Eastside Centre Ct, Ste 6, Mountain Home, AR 72653
800-980-OGRR (6477)
www.ogaugerr.com

×
×
×
×
Link copied to your clipboard.
×
×