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This just stinks all the way around… I hope everything turns out ok in the end…

From a mechanical standpoint I’m kind of surprised at the way the smoke box front failed. I would assume it would be made of sheet steel, but it appeared to crack like cast iron would… I would have expected it to bend/tear…

A lot of heat can make metal brittle, including cast iron. The smokebox is one of the hottest parts of a steam engine hence why it has its own special silver coating.

@Hot Water posted:

Welding cast iron is NOT easy, especially a piece, or pieces, that size. They will simply have a new one cast. The Strasburg Shop is VERY resourceful.

I was just thinking in terms of getting it to stick together good enough to be used as a pattern. I know it would not survive in service… I suppose they could also make new patterns from drawings (if they exist). The bottom line is that the guys at Strasburg actually know the right way to make a new smoke box front, and I’m just speculating…

@naresar posted:

I don't really have much additional insight except to question what expectation the crew had of the switch being lined correctly.  Yes they should have been looking as well but were they aware that there could be any issue.

One question though, does anybody know if 475 is superheated.  Couldn't find anything online in a quick search,

Despite having outside steam pipes the 475 is not superheated.

Stuart

@Hot Water posted:

No, the smoke box front is cast iron, NOT sheet steel.

Besides them recasting a new smoke box and whatever time that would involve, would there be a complete examination of the smokebox, make sure that there is no damage to the boiler, etc? Yeah, the shops are very resourceful at Strasburg. I did a tour there back in 2019 which was very informative. They do a lot of outside work for other people as well as anything in house.

You live or die by the sword:

Rule 6.27

When a train or engine is required to move at restricted speed, movement must be made at a speed that allows stopping within half the range of vision short of:

Train

Engine

Railroad car

Men or equipment fouling the track

Stop signal or derail or switch lined improperly

The crew must keep a lookout for broken rail and not exceed 20 MPH.

Comply with these requirements until the leading wheels reach a point where movement at restricted speed is no longer required.




There is no excuse for what happened. Regardless of the switch not being lined for that movement, the Engineer was responsible for WATCHING ahead of him SEEING that the switches were lined properly IN ENOUGH TIME TO STOP. (Instead, he was lolly gagging and waving at the passengers.)

You must ALWAYS move in yard/switching type situations watching in the direction of travel and checking switches and watching for close clearances. From what can be determined from the video clips, he had time enough to SEE the switch and safely STOP. It would have then been a situation of lining the switch, mention the foul up to the MOW fellow that screwed up, and no damage, no one fired/disciplined. Compliance with the rule did its job.

Handling trains and running engines, regardless of a tourist operation or what, is serious business and it is NO time to lose situational awareness. Even in tourist service, it's not just a big Lionel set... poor judgement can kill or maim.

In all my years of handling trains/engines in restricted situations, I never once went past a stop signal (flag, fussee, etc), stop test, or ran into an obstruction, or a switch lined improperly, etc. It can be done but you've got to keep your head cut-in at all times.

This was totally uncalled for. At the least, unpaid time off should be served for this incident.

Andre

Last edited by laming

I am very happy no one was hurt in this crash. At least that is what is known right now. Those videos were very hard to watch. So Like what was said above so many folks love the SRR myself included.It's good to know they will get back on their feet.

While The engineer has to held accountable I hope that he doesn't get permanently fired over this especially if he has an unblemished record until now. Anyone can make a mistake. I am sure he feels terrible and I am sure he learned a very serious lesson.

Last edited by Hudson J1e
@superwarp1 posted:

Anyone notice that the Virtual Railfan Paradise, PA feed has been shut down and no posting from them about the accident?

I'd figure that they will be investigating, writing up reports, etc. They may release something later on, maybe after the FRA investigation is done. Hard to say, I just know that when I worked for my last company(nothing to do with trains), accidents of any kind would take a few days to get everything documented as to what happened, and then action plans would be put forth from whatever the finding were. I would expect nothing but a serious tone as with any type of investigation regardless of how minor. I'm not saying this is minor, as any accident involving equipment is major.

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