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I have the MTH O scale operating Crossing Gates signal set  30-11012 and they are very scale looking and operate great but with  loud gear grinding noise even after packing with grease that helped a little , Those and my Atlas oil rig are getting switches  installed  so I can turn them off and don,t have to listen to them, unless I can locate some other brand that are not so noisy.

 

They are an attention getter but not for the right reason.

 

I have entertained thoughts of installing a below the layout cam to operate them and gut out the signals or just scratch build complete new gates and operate with the cam below..

 

any suggestions or experiences to share ?

 

Jim Warren, Ohio

Last edited by Jim Teeple
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Jim: 

I have (4) set of these gates. It is unfortunate they make so much noise.  I've had them apart and oiled them heavily with little change in the sound.  They are also notorious for failure.  The small plastic gear that is pressed on the motor shaft splits, though this can be fixed with CA (super glue). The limit switches, two screws on the back of the control panel may also need adjusted.  Top screw is the upper limit.  Bottom screw is the down limit. Clockwise on both should shorten the travel.  They are very nice looking crossing gates.

 

The verticle worm screw design would lend to just extending the shaft to below the table. The motor can also be removed from the base.  Though the motor is most of the noise.

 

Last edited by Mike CT

I too did not like the noise these realistic looking gates made so I took them apart and removed the little motor and most of the gears leaving the worm gear that rotates the vertical shaft inside.  Then I installed a small robotics gear motor that turns about 75RPM to the shaft with a flex drive.  The wiring had to change since the motor I used was DC but now the gate comes down nice and slowly without much noise.

Originally Posted by Kenai:

I too did not like the noise these realistic looking gates made so I took them apart and removed the little motor and most of the gears leaving the worm gear that rotates the vertical shaft inside.  Then I installed a small robotics gear motor that turns about 75RPM to the shaft with a flex drive.  The wiring had to change since the motor I used was DC but now the gate comes down nice and slowly without much noise.

Hey Kenai - that sounds like a neat project.  It would be great if you could post a full how-to with the parts you used.

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