Well, when all fails, move in another direction, so I decided maybe there was not too little, but too much smoke fluid, maybe from my previous tries, so I inverted loco and removed the pilot truck and screw that seems to go into smoke box assy and a lot of fluid drained out. I blew in some (very low pressure) compressed air into that screw hole, thoroughly wiped away the truck and smoke box and let it sit for several hours to drain. I reassembled and put it back on the track, adding no fluid and it smoked very well, like I had never seen it do before! Evidently a little fluid goes a long way in these. I am so happy with it now. These engines are awesome and can be bought so cheaply (I paid $180 in C9/P9) as evidently Lionel way overproduced them. And they do not have circuit board issues that I have heard plague some recent China MTH and LL engines!
Thank you all for your inputs. See you at York. 18040 is now on my list. Valete!