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A few weeks ago I posted concerning a cracked worm gear in one of the motor trucks of a WBB scale FA-1. I noted that Northwest Short Line (NWSL) supposedly had the correct replacement gear and promised a follow up after receiving the part from NWSL. A link to the earlier post is included.

https://ogrforum.com/...acked-wbb-drive-gear

The NWSL replacement gear arrived yesterday and I’m happy to report it is an exact match! I installed it in the motor truck this morning and it works perfectly.

I’ve included several photos and a video below. Number 1 is of the packaging from NWSL showing the part number. Photo 2 is a visual comparison of the original WBB brass gear (top) and NWSL replacement (bottom). Photo 3 shows the gear installed in the WBB motor truck. Last one is a short video of the motor truck under load.

Curt

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Last edited by juniata guy
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Thanks Pat!

I’ll qualify this by stating I only wish I had the tools that you have on your workbench!

I used a small flathead screwdriver and hammer to tap the shaft from the compression collar (or nut, if you prefer) that holds everything in place. Once the collar was removed, I used the same tools to remove the shaft from the truck. The cracked gear easily came off while removing the shaft.  I next positioned the replacement worm gear in the slot in the truck and slid the shaft back into place and partially through the worm gear. I then placed two small flathead screwdrivers alongside the gear on the collar side of the shaft (to hold the gear in place) and using a hammer, tapped the shaft through the gear till it was properly positioned. I reapplied the compression collar using a large pair of pliers. It goes without saying that care must be taken to make sure the brass gear on the side of the truck properly meshes with the drive gears on the side of the truck. The compression collar must also allow some “play” in the shaft or the large drive gear may bind with the others.

If I had to do these frequently, I’d probably create a shim or backstop to hold the gear in place while I tapped the shaft through. The two screwdrivers worked but, it was awkward. I figure cutting enough from a large, thick flathead washer to allow it slip over the shaft should work as a backstop of sorts. This would then be removed once the worm gear is properly seated.

Curt

Last edited by juniata guy
@juniata guy posted:

Thanks Pat!

I’ll qualify this by stating I only wish I had the tools that you have on your workbench!

I used a small flathead screwdriver and hammer to tap the shaft from the compression collar (or nut, if you prefer) that holds everything in place. Once the collar was removed, I used the same tools to remove the shaft from the truck. The cracked gear easily came off while removing the shaft.  I next positioned the replacement worm gear in the slot in the truck and slid the shaft back into place and partially through the worm gear. I then placed two small flathead screwdrivers alongside the gear on the collar side of the shaft (to hold the gear in place) and using a hammer, tapped the shaft through the gear till it was properly positioned. I reapplied the compression collar using a large pair of pliers. It goes without saying that care must be taken to make sure the brass gear on the side of the truck properly meshes with the drive gears on the side of the truck. The compression collar must also allow some “play” in the shaft or the large drive gear may bind with the others.

If I had to do these frequently, I’d probably create a shim or backstop to hold the gear in place while I tapped the shaft through. The two screwdrivers worked but, it was awkward. I figure cutting enough from a large, thick flathead washer to allow it slip over the shaft should work as a backstop of sorts. This would then be removed once the worm gear is properly seated.

Curt

I’ve fixed several of these as well, and you nailed it, ….I’ve fashioned the back stop shim from a piece of milled aluminum that basically looks like a miniature tuning fork. I don’t use the press for these either. I prefer the sneak up on it tap, tap, tap approach too,….if I feel I tapped and hit solid I know to stop…..I’m skeptical on pressing these. They sure look like they can go sideways quickly if you’re not careful,…..nice job!!

Pat

I’ve only had to replace a WBB motor truck on an engine once previous to the worm gear on my L&N FA-1 cracking. Having experienced only two cracked gears out of 30 two motor engines over the years, I probably wouldn’t characterize this as being a common problem.

Obviously simply replacing the entire motor truck would have been easier (and more expensive) had Bachmann any available but; the repair really wasn’t that difficult once I learned NWSL had the correct replacement gear. And honestly, as Rod alluded to in his post, it’s a nice feeling of accomplishment to repair something and bring it back to life. It’s just another aspect of the hobby.

Curt

Last edited by juniata guy

The issue of cracked gears seems to be a "common" issue on specific models.  For instance, the Century Club TMCC PRR Shark A-A had that problem, I ran across it several times with repairs.  Then I bought the Century Club A-A Sharks at York a few years ago.  It had not one, but two cracked gears.  As it turned out, I could actually still buy the trucks from Lionel parts.  I also discovered a different power truck has the same gear, so I bought a couple of spares.

Some of the Early MTH PR E-8 had this issue, long ago I found MTH had that gear as a part.  Once assembling though I use a vice with spacer to press back on gear or wheel, with a center spacer that ensures one side of the vice is pressing on the axle of the wheel or gear you don't want to have move on the axle.  Vice gives nice precision movement, as I like to avoid impacts when reassembling something like this.  G

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