AS some of you may remember I have on occasion been trying to breath new life in a lionel 4-4-2 , cab #8304. The engine was running balky and had the old two position mechanical e-unit. So the first thought was to replace the e-unitwith an electronic one. This turned into a mess trying to get a modern Dallee reverse unit to fit under the shell. After I finally got it to work there was no way to make enough room to re-install the trailing truck. Anyway , I really wanted to have a dc motor. I tried to find one I finally decided that it would be easier to just buy a modern version and transplant the guts to my shell. Great plan, lousy consequences...
The donor was from a broken up lowe's nascar set.
Despite the 40 year difference, the frame itself is the same and the smoke unit is identical. The way the smoke unit is mounted is different but it didn't matter. The head light is now an led that is head on with hot glue and there are shut off switches for the smoke unit, and a lock out for the direction.
So problem #1 was that the hole for the fork bracket that holds the motor frame to the front of the shell was not tapped. Not surprising since the original had a self-tapping screw. Not wanting to force it I bought a tap and threaded the hole. I also picked up a hot-glue gun to mount the headlight and switches.
The inside of the old shell needed to be hollowed out a little bit with a dremel because the new motor stuck out a bit further. I thought there wasn't going to be enough room until I realized I could move the little capacitors around some. That made way for the shell to fit but one of the capacitor was sticking out below the shell. So for this one I lifted it off the rest of the solder connections, added a small wire to one side and reattached the wire in place of the original connection. this allowed for the shell to fit without further material removal. After that it was gravy - hot glue in the headlight circuit, reassembly the engine, and hot glue the switches to the inside of the shell.
So now it's time to sit back and be proud of myself, so I thought. I set the engine on the O31 test oval and it made about three laps before it suddenly slowed down. I thought it was just something mechanically tight as this happened in a curve. So I apply a little more power and it make about 4 or 5 more laps then the breaker trips.
At first I think the lead truck must be off or something but no - everything looks good.? First reset of the breaker - smoke coming out the old e-unit slot - not good.
So I think something must be grounded inside the shell. I take the off, tape the smoke unit to the forks and put it back on the track. Sure enough the reverse board is smoking. I was foolish enough not to do any test laps before staring the transplant so I don't know if the board failure was bound to happen anyway or is the result of something I did.
Anyway I thought I'd share my misery. I'm just trying to bring a sentimental toy back to life and getting thwarted at every turn.
here's the pictures just for fun.