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One of my modular group colleagues recently got his pre-odered Legacy Berk. At home he runs Blue Tooth on a moderate sized layout.....about 6x12".

While the engine is traversing the loop, it loses chuff. Cyclying through reverse restores chiff. Command control is not effected.

Brought to the club layout. It did the same. I reprogramed the engine to #25 with the Cab1L.  It occurred again though less frequently.

Brought it to my home. The layout is a 14x22 L-shaped loop.

I have a Base3 and ZWL. Track is cleaned (rarely use smoke). Ross track and switches. Lots of power drops and both grounds wired. When it happend here, we cleaned the track (again.....and, it was pretty clean), and, cleaned the Berk's wheels and rollers.

It still happened.  I followed it around to catch it and I edited the video to the segment where the chuff goes out and we restore it by reversing direction.

For reference, my Legacy Atlantic and Legacy mogul ran flawlessly this week and earlier today.  (videos can be seen in this week's Weekend Photo Fun).

My colleague, Jim, will be calling Lionel and sending them this video......

I'm interested in what might be going wrong......

Peter

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Last edited by Putnam Division
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Peter, my guess is the IR receiver  is getting out of alignment. The sounds emitting from the tender are the same sounds you will here when the tender is placed on the track by itself. Reversing the engine is probably allowing the drawbar to reseat itself. It’s tough to tell in the video  but it looks like the drawbar on the tender maybe sagging allowing the IR receiver to get out of align. The hooked portion on the engine side seems to be riding higher.

@Dave_C posted:

Peter, my guess is the IR receiver  is getting out of alignment. The sounds emitting from the tender are the same sounds you will here when the tender is placed on the track by itself. Reversing the engine is probably allowing the drawbar to reseat itself. It’s tough to tell in the video  but it looks like the drawbar on the tender maybe sagging allowing the IR receiver to get out of align. The hooked portion on the engine side seems to be riding higher.

I agree. At about 10 seconds into the video it would appear the draw bar is not fully seated. I have found some tender draw bars are out of tolerance forcing only a fraction of the loco's draw bar to seat. I would suggest taking a small file and open up the hole on the tender's draw bar.

@Dave_C posted:

Peter, my guess is the IR receiver  is getting out of alignment. The sounds emitting from the tender are the same sounds you will here when the tender is placed on the track by itself. Reversing the engine is probably allowing the drawbar to reseat itself. It’s tough to tell in the video  but it looks like the drawbar on the tender maybe sagging allowing the IR receiver to get out of align. The hooked portion on the engine side seems to be riding higher.

Dave…..the video is 2.5 minutes long…..I will look at some of the segments on the straghtaways to see if I have tether shots.

Peter

From my modular colleague, Jim:

The Forum was spot on! Tender draw bar was the issue.

Upon close examination of the tender’s drawbar, could see a slight downward tilt. Made upward adjustment and placed on the track, ran  45 minutes straight at various speeds without any drop of sound whatsoever.

Berk is alive and doing well! Thank you for all the help today with the run time and post on the forum. I would also appreciate it if you would thank the folks on the Forum for me.

Jim

Thanks to all who commented!

August will be 25 years on this site for me, and this generous sharing of knowledge still keeps teaching me things!

Peter

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