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Today at approximately 11:23, EST Strasburg 475 struck a piece of standing MOW while running around their train.

Switch appeared to be lined for the siding/track that the MOW equipment was on, but also a violation of restricted speed by the engine crew… smoke box was punctured by an excavator arm.

No information on injury.

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Who left the switch lined for the siding? Where was the conductor? I could understand how the engineer might not have been able to see which way the switch was thrown. I can only imagine what the engine crew felt like when they realized that the engine was headed down the wrong track…



This is not good…

I hope there isn’t damage to the cylinder casting!

Hopefully no one was hurt and the damage can be repaired. I didn't see any steam or smoke escaping from the front where the damage is, so hopefully that means it is more patching the shell than anything else (maybe wishful thinking on my part, and I claim no expertise on the design of this or any steam locomotive). 

I am as confused as some of the other posters. Was the engine supposed to push the cars, and instead got diverted to the siding? Or was the engine doing a move around to position itself at the head of the cars on the left (I don't know if this siding is just a siding or does it end up connecting to the track ahead of the cars? ). If it was just simply they were sent to the siding by accident, then the question is did the MOW crew leave it thrown?If it was a run around, then how come the train crew didn't see the MOW equipment when they threw the switch?

In the end it is just sad. I am sure the train crew at the least got shook up and maybe banged around a bit, it was moving enough to cause a jolt I am sure.

Part of the problem was the conductor at least and maybe the engineer I can't really tell in the video, was hanging out the window waving to the people in the coaches. I realize they meant well, but ultimately it's the crews responsibility to make sure the track ahead is clear and lined. Restricted yard speed States being able to stop in half the distance of sight.

@bigkid posted:

I just realized that the MOW was on a spur off the passing siding and the switch was thrown to go straight. I suspect the MOW people left the switch in that position and the train crew wasn't looking. At this point I leave it to investigators to figure out.

I don't think it will take super sleuth investigators to come to those conclusions either...

I don't really have much additional insight except to question what expectation the crew had of the switch being lined correctly.  Yes they should have been looking as well but were they aware that there could be any issue.

One question though, does anybody know if 475 is superheated.  Couldn't find anything online in a quick search,

This just stinks all the way around… I hope everything turns out ok in the end…

From a mechanical standpoint I’m kind of surprised at the way the smoke box front failed. I would assume it would be made of sheet steel, but it appeared to crack like cast iron would… I would have expected it to bend/tear…

No, the smoke box front is cast iron, NOT sheet steel.

I watch that cam all the time. The SRR has been replacing the interchange siding with NS west of the highway overpass. The excavator has been parked on that short spur in front of the old wreck crane for several weeks.

Looks like an unfortunate instance of complacency by the engine crew since that switch is rarely ever moved. The MOW crew has some explaining to do. Fortunately no one was hurt.

Sad to see 475 get punched right in the nose.....

Bob

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