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Like many others on this forum, I get a great deal of pleasure simply repairing trains. This is my experience repairing a 342 Culvert loader that my Dad bought for me for Christmas sometime in the late 50’s or early 60’s. If you are experienced and masterful in this notoriously touchy repair, I hope you will indulge me while I share my experience with others.

All the pieces were there except for the string (well, I had a small piece of it) and the spring that supplies tension to the string. I bought the string from Jeff Kane just because the requirement is for a wax free nylon string, something I did not have on hand. But I forgot to order the spring! So I used a motor brush spring. It was close, but had the disadvantage of quickly stretching over time as the vibrator tugged and pulled on it.

After a thorough cleaning and reassembly, it sort of semi-worked – it was painfully slow with very little power, many times requiring a push to keep it moving. Adjusting the tension didn’t seem to help - as I added or reduced tension on the string/spring combo, it ran worse.

Finally the light bulb went off and I realized that this motor relies on the fact that when the vibrator moves rapidly toward the drive pulley & gear, it reduces tension on the string and lets the spring pull things back toward itself, but in so doing, it does NOT rotate the drive pulley because of the reduced tension – exactly how it’s supposed to work. When the vibrator pulls away from the drive pulley, it puts tension on the spring and string, and causes the drive wheel to rotate. The fact that mine had little power suggested the string was slipping on this part of the duty cycle. So I removed the drive pulley and thoroughly cleaned it with alcohol – there was plenty of oil and grease to go around, and I even found the brand new white string had black splotches where some of the oil had found its way. So being cheap, I cleaned the string with alcohol.  But oddly, that alone didn’t fix anything. I next roughed up the inner groove of the drive pulley with the edge of a very small flat file. BOOM! That did the trick! I guess many years of the string rubbing on the inner groove of the drive pulley had worn it quite smooth, affording almost no traction. Immediately I had a ton of speed and power!

As I mentioned earlier, the brush spring stretched pretty quick, so in very short order I lost a lot of my newly gained drive power. Putting the tip of a screwdriver in between the center coils of the drive spring, then pulling and pushing to change the tension while watching the vibrations of the string, quickly revealed that lack of tension was the problem. With insufficient tension, I could see the string vibrating wildly. As I pulled on the spring to increase tension, the string vibration quickly went away, speed and power resumed. So I temporarily used another small piece of string to tie off two or three turns on the spring - BAM! Problem solved, power returned.

IMG_0682

BTW, Lionel says to make that tension adjustment, bend the tab where the spring is attached until things operate well, but the tab is stiff and awkward to reach with normal hand tools. Lionel’s service manual also provides their process for installing a new string. But this was my temporary solution. I assume the spring will stretch again, so hopefully the spring I will get from Jeff in a couple of days (yep, ordered it!) will work better.

Then I had the other “normal” problem that everyone has - as the conveyor assembly  would start moving back to grab another culvert, instead of smoothly releasing its load to drop straight down into the gondola, it hung on for just a split second, making the culvert drop a tiny bit late, off-center and crooked in the car.

The solution for me was to cut a small strip of cloth electrical tape (the kind your grandfather used) and apply it to the top, outer portion of the beam, right where the outer roller on the conveyor reverses on each run. This creates friction for the outer roller on the conveyor, holding it back and forcing the release of the culvert right on time. I went from a 1 in 7 correct drop to a 7 out of 8 correct drop instantly. Adding a 2nd much shorter piece of tape on top of the first piece, just inside of the where the outer roller stops did the final trick – it forms a very small step that will aid in making the release work correctly.

Tape Application

I should point out that when I cleaned the conveyor, I got rid of all oil & grease that the kid in me had applied years earlier. This is one of those devices where oil is really not needed and only serves to gum things up down the road. I added a small bit of graphite to both rollers initially, but ended up cleaning that off the outer roller as part of my attempt to add a small amount of friction and drag to force an on-time release.

I hope this helps someone else who has spent a few hours monkeying with a cantankerous accessory like this one!

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Images (2)
  • Tape Application
  • IMG_0682
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Regarding the string motor:

Lionel used the string motor in a number of accessories.
As you found, the string and pulley must be absolutely clean.
I think that if you had the correct spring, you would not have needed to rough up the pulley to make it work.

I have never adjusted a motor by bending the bracket. I have always been able to make fine adjustments by grabbing the end of the string next to the lightly crimped eyelet with a pair of pliers (edge resting against the eyelet) and twisting the pliers just a bit to tighten further.
The string can also be loosened this way if the crimp isn't too tight.
When adjusted, tighten up the crimp.

thanks for an excellent explanation of how to repair and adjust the older Lionel  accessories. would like you too explain if you have ever ran into problems with the  horse and cattle cars that always seem to vibrate too much or too little and the platform sits on  rubber bumpers that get soft or ware out . have you had any success with these. I have several and  they never seem to work 100% and even if the cattle or horses work threw the Carrol but the car door does not drop down low enough and the horse or cattle can't enter! ever ran into  that issue ? would like to see a forum about this when you get time!

 thanks

Alan 

Last edited by Alan Mancus
C W Burfle posted:

Regarding the string motor:
I think that if you had the correct spring, you would not have needed to rough up the pulley to make it work.

I have never adjusted a motor by bending the bracket. I have always been able to make fine adjustments by grabbing the end of the string next to the lightly crimped eyelet with a pair of pliers (edge resting against the eyelet) and twisting the pliers just a bit to tighten further.
The string can also be loosened this way if the crimp isn't too tight.
When adjusted, tighten up the crimp.

I suspect your comment is spot on regarding having the correct spring. I will know in a couple of days when a correct spring arrives.

I like your technique for adjusting string tension. Unfortunately as a youth, I must have performed indelicate surgery on the crimp - it was a wee bit mangled, and a knot seemed to be the easier solution.

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