My experience was with a conventional Rail King GS-4. So, I had no voltage issues. After removing the body shell and smoke unit, when I was ready to test the fan, I plugged its connector to the circuit board and applied power to the locomotive rollers.
I saw that the fan wasn't spinning. I heard no sound from the motor. I pulled the fan rotor off and applied power to the rollers with all of the wiring attached and felt the shaft with my finger to make certain that it wasn't rotating. It wasn't, which isolated the problem to the motor or the plug connection on the circuit board.
Two tiny tabs held the motor end cap on and by straightening them the motor cap came off. After cleaning everything and carefully reassembling the small parts, the motor worked fine. I pushed the fan rotor back on, reassembled the unit and it smoked poorly. I took it apart again and repositioned the wick and it worked fine. The squeal the fan rotor was making prior to the procedure also disappeared. Again I thank Ingenierio #1 for posting this information originally.
If you do not want to get into it this deeply, you got two excellent suggestions -- the spray electrical cleaner Gunrunner John suggested might well flush out any smoke fluid and reestablish electrical flow, or you could follow Paul S.'s suggestion and just buy a new motor for $6 if you have determined that the motor is indeed the problem.