Skip to main content

I thought someone might find use for a gadget I developed so I’ll describe it and put up some PICs.

 

First a little background. After running Lionel PWC NW2s the Plywood Empire Route recently acquired a couple MTH PS3 SW1500s and a new era has begun. With speed control these engines make switching moves at a [scale] walking speed. Unfortunately Lionel “claw” couplers require a lot of force to couple so more like an Olympic sprinter’s speed is needed thus defeating the realism of slow-speed switching. A switch to Kadee couplers would solve the problem BUT the only space available for a return loop/interchange track/fiddle yard requires an O31 circle so truck-mounted couplers must be used and no one yet offers a way to mount Kadees on MTH freight trucks. So I’m stuck with crash-coupling claws. What is needed is brakes on standing cars so I assembled and installed several such devices.

 

                                 IMG_3384

 

                       IMG_3383

The basic bit is a Circuitron Tortoise slow-motion switch machine usually seen on HO pikes. It actuates a 5/32" brass tube which is fitted inside a larger 3/16" piece of tubing.  The 3/16" tube is friction-fitted and hot glued and the whole assembly is attached to the underside of the plywood decking. Installed in the roadbed adjacent to an electromagnetic uncoupler it looks like this:

 

               IMG_3378

Seen here in the lowered position.

              IMG_3377

And here in the raised position.

 

            IMG_3379

Here it is seen in position to stop a car from moving while a car comes from the left and pushes the coupler slowly closed until it locks. No more crashing cars together! Switching is now much more like the real thing on the Plywood Empire Route.

 

Video of the gadget at work:

                     

                     

Lew

 

Attachments

Images (5)
  • IMG_3384
  • IMG_3383
  • IMG_3378
  • IMG_3377
  • IMG_3379
Videos (2)
IMG_3386 (1)
IMG_3387 (1)
Last edited by geysergazer
Original Post

Replies sorted oldest to newest

I'm glad to see people are going to use the idea! Like all such projects I thunk and I thunk and then it came together quite quickly. 

coach joe posted:

Lew that's a great idea.  Could you have placed it closer to the magnet so the car doesn't roll as much or did you purposely leave room for six wheel trucks?

Yup, they are placed to allow for slight variations in exactly where the uncoupling tab is located on the underside of the truck. 

Lew

Big_Boy_4005 posted:

Sold!

I was thinking of something like that for my hump yard to catch the cars at the end of the bowl tracks, so they don't foul the switches. I even have a half dozen Tortoises on hand for the project. You made it look easy. 

 

Elliot, it really is an easy project. Once the first one is tweaked to account for your roadbed thickness, decking thickness and track height you can bang them out pretty quick. One thing I ran into with the K&S brass tubing was a variation in diameter such that a couple of the 5/32" inside "plungers" had to be chucked in my drill-motor and sanded to a slightly smaller diameter to slide effortlessly in the outer tube. 

Lew

For anyone wanting to duplicate the device a couple details might be helpful.

 

The 5/32" plunger needs to have a relief cut (Dremel tool) from the backside to permit free movement of the piano wire actuator:

                 IMG_3416

 

       IMG_3383 [1)

Not a very good pic but you can see that the piano wire actuator is thus free to pivot in the plunger.

 

Regarding control, Circuitron's instructions were followed. 14VAC accessory power from a Z1000 was employed by using 5A diodes and a SPDT miniature toggle switch:

 

                    IMG_3436

 

                   IMG_3438

Flipping the SPDT switch reverses the polarity of the 14V half-wave DC being applied to the Tortoise machine thus causing it to reverse direction and stall in the opposite position.

 

Lew

Attachments

Images (4)
  • IMG_3416
  • IMG_3438
  • IMG_3436
  • IMG_3383 (1)
Last edited by geysergazer
gunrunnerjohn posted:

Clever solution to the issue.

I've taken to disassembling the couplers and smoothing all the inside latching surfaces.  You can usually get Kadee-like performance if all the interior surfaces are polished.

Obviously, your solution appears to be a lot less work if you have a ton of locomotives and rolling stock.

I was desperate for a quick&dirty fix but  that is going to be my next step. There sure is a lot of variability in coupling performance of Lionel-style couplers. Spring tension also seems to vary, especially of the horizontal coil spring that pushes the latch-bar against the knuckle.

Lew

gunrunnerjohn posted:

Clever solution to the issue.

I've taken to disassembling the couplers and smoothing all the inside latching surfaces.  You can usually get Kadee-like performance if all the interior surfaces are polished.

Obviously, your solution appears to be a lot less work if you have a ton of locomotives and rolling stock.

Very true. I can’t understand why the manufacturers can’t do this as an improvement to their product. That would be total quality improvement.

For years the standard solution has been Kadee's, kudos to you for thinking out of the box!!  However, I want to add that there are differences in geometry among postwar Lionel, MPC, modern era, K-Line, Weaver, and MTH couplers.  As an operations modeler, @Bob (Pennwest) explored a lot of this and wrote about it a while back.  He spent hours tuning his couplers.  I suspect the mfr's don't do it because of the time and labor involved.

Bottom line- if the geometry of the mating couplers doesn't complement each other in a certain way, they won't close together no matter how much force you apply.  So if you're determined to do this type of operation, I would find ONE brand of rolling stock or trucks that works well, and stick with it.  (If you're willing to cannibalize,  you can always install one brand's truck on another brand of car.)

Thank you for sharing what could become a very valuable addition to operations-oriented layouts.

Last edited by Ted S
gunrunnerjohn posted:

My personal observation has been a lot of the issues are the molding lines on the moving parts of the couplers.  I have gotten a few electrocouplers to couple with hardly any pressure while still keeping them reliable for running.

Yes, the electrocouplers on my two MTH SW1500s work beautifully. They click shut at a nice slow coupling speed. I would pay a premium for freight trucks that would work as smoothly.

Lew

Ted S posted:

For years the standard solution has been Kadee's, kudos to you for thinking out of the box!!  However, I want to add that there are differences in geometry among postwar Lionel, MPC, modern era, K-Line, Weaver, and MTH couplers.  As an operations modeler, @Bob (Pennwest) explored a lot of this and wrote about it a while back.  He spent hours tuning his couplers.  I suspect the mfr's don't do it because of the time and labor involved.

Bottom line- if the geometry of the mating couplers doesn't complement each other in a certain way, they won't close together no matter how much force you apply.  So if you're determined to do this type of operation, I would find ONE brand of rolling stock or trucks that works well, and stick with it.  (If you're willing to cannibalize,  you can always install one brand's truck on another brand of car.)

Thank you for sharing what could become a very valuable addition to operations-oriented layouts.

Yup, every freight truck on the Plywood Empire Route is the MTH version with the uncoupling tab hidden under the truck. Even with this degree of standardization I ran into a couple couplers that simply wouldn't lock when mated against similar couplers. Close examination showed the coupler body to be shaped slightly differently than all the others. They went in the "to-do-later" box 

Lew

gunrunnerjohn posted:
geysergazer posted:
I would pay a premium for freight trucks that would work as smoothly.

Lew

I suspect that's the only way you'll get them!

An alternative would be for someone to manufacture something like this:

      IMG_7437.PNG

An adapter to install Kadee couplers on MTH freight trucks. It looks like 3D printing wouldn't work because insufficient strength so it would have to be lost-wax cast in metal.

Lew

Attachments

Images (1)
  • IMG_7437.PNG
M. Mitchell Marmel posted:

Excellent idea!  I'd recommend some sort of interlock so that a moving train doesn't hit the extended post.  Also, I'd recommend some sort of quick-change capability so that, if a goof occurs,  the post can be easily replaced.  

Overall,  a brilliant concept!  Kudos! 

Mitch

I've tried to figure out an interlock but it won't work because the track has to be powered to enable the very switching moves the device is there to enable. Of course the Tortoise machines have auxiliary switch contacts for such purposes. Since I have two of the devices installed on the mainline I'm going to wire red panel lights to those contacts to warn when the mainline is blocked. That is a project for another day when I getaroundtoit and finally construct a proper control panel with a track schematic and switches to operate track switches, uncouplers and track blocking devices.

Lew

Wow this is a great idea.  I think I would build on Mitch's comments and make the post out of something more flexible than a brass rod so cars could accidentally run over it without a derailment or damage.  The post just needs to hold a static car in place, so something like a plastic coffee stirrer (the little straw kind) perhaps with a few cuts to provide a hinging effect to encourage bending might be sufficient.  It could hold car(s) from moving for coupling but bend if it got run over by accident. 

Dale

I just installed a variant of the device. I had to work around a couple deck joists and an L-Girder by using a longer casing and a much longer plunger to get below all the woodwork. The only necessary elements of this thing are the plunger, the casing it slides in and of course the Tortoise switch machine which animates the plunger. In this case the casing passes right through a girder flange in order to guide a much longer plunger. A pic is worth a thousand words:

 

                    IMG_3456

Lew

Attachments

Images (1)
  • IMG_3456
Mixed Freight posted:

Just a note, but for the extremely frugal, some sort of a bellcrank and pushrod assembly could undoubtedly be easily rigged up to take the place of a Tortoise.

Ya, I thought a bit about that but the Plywood Empire Route is a sit-down operation with hip-walls only 43" high. OTOH a walkaround pike would be well suited to pushrod actuation of these car-stoppers.

Lew

As a footnote to this project, the need to find a home for the miniature toggle switches used to control the car-stoppers prompted me to construct a control panel incorporating all control functions (except throttle as that is with hand-helds) in one place:

        IMG_3563

On-off-on toggle switches marked "U" control the various Fastrack remote uncouplers. On-off-on toggle switches marked "S" control the various track switches. The unmarked on-off toggle switches control the various car-stoppers. The indicator lights show track switch position. Although a track schematic would be nice I chose to go for minimum footprint and ended up with 4"X20" for my small pike. 

 

By way of re-hashing, the Tortoise machines that actuate the car-stoppers are controlled by SPDT momentary on-off-on miniature toggle switches which polarity-switch the power to the machines:

On-off-on momentary switches used to control Fastrack track switches are wired thus:

      IMG_3561

Bi-color LEDs provide route indication. Very simple wiring with a 470 Ohm resistor protecting the LED.

That's it, good people.

Lew

Attachments

Images (2)
  • IMG_3563
  • IMG_3561
Last edited by geysergazer

Thanks, Greg. Agreed, that for a tutorial I need to get better pics and more of them.

For example, one problem I didn't get into is that the fit between the K&S 8128 and 8129 brass tubing is really too tight (actually a manufacturing tolerance issue because the fit varies from one piece of tubing to the next). My solution was to chuck the 5/32 (8128) tubing in my drill motor and apply 220 grit paper followed by 400 grit to polish, thereby reducing the diameter a couple thousandths. I don't know of an elegant solution so I would need to include pics of that process.

Lew

Last edited by geysergazer

This reminded me of a tactic I used while switching on my test track--sticking a finger behind the wheel of the stationary car being coupled to, making it a chock of sorts to keep the car from moving when being coupled to. A sticky rubber wedge on a stick could potentially do the same thing.

I wonder if an R/C servo and servo tester could be a cheaper alternative to a switch machine (although to be honest, I haven't priced the switch machine used here), using a single tester routed to various servos via selector toggles.

I can vouch for the complication of variable geometry of various brands' couplers, recalling my thread on tuning a Menards 24-flatcar set so their couplers would behave properly.

---PCJ

Last edited by RailRide

Add Reply

Post
×
×
×
×
Link copied to your clipboard.
×
×